I started the strip down to asses the damage. Before I started I turned on the fuel pump and found fuel coming from the rail! On closer inspection I found the fuel rail bolt half hanging out and the injector had come out of the rail. So at least I had found the origin of the leak. The full diagnosis it turns out is that the injectors are slightly too long for the rail to sit onto its mounting posts on the inlet manifold, as a result, when the rail is bolted down, it tries to squeeze the injectors and put the rail under tension which should deffo not be the case! It turns out it had actually ripped the thread out of the manifold because of the tension! So I know the full route of the cause which is the very important so it doesn't happen again!
The rail will be refitted with a washer between the mount and rail which will space it enough that it clamps the injectors but with no tension!
strip down
Tried a few different things, panel wipe, brake cleaner, sponge etc. I then got the acetone out and this stuff was magic!! Tried it on the boost pipe and strut brace...
Mint!
Quick look at the bay
You can see
loom charred at the back and engine loom
hoses discoloured
powdercoat tarnish
paint black
header tanks black
powder hiding around
So I set to work with the Acetone and quick detailer after and this was the result
Pretty god damn good in my opinion!!! I am a very lucky and happy boy! The only things that wouldn't clean up are the header tank and brake fluid res.
Also, seems like the slam panel and bonnet in the same area were super heated and it melted the paint!
Deffo not the worst thing in the world, I can repaint the scuttle in winter and I actually wanted to repaint the bonnet anyway because there is a dent in it. Do that in winter too
So the rebuild began, fuel rail cleaned up, Injector were flow tested, no issues, new o rings fitted. This time, the saftey clips for the injectors were lockwired to the rail to stop them coming out if the rail every came loose again!
I forgot to take a photo, but the fuel rail is now drill n tapped from M5 to M6, it is now nut and bolted and the bolts are lock wired together! This rail is never coming loose again
Inlet cleaned and refitted. Acetone is a miracle worker!
New air filter and the whole car is back together the night before VBOA rally!
I warmed it up, gave it a foot full to the roundabout and back. Test drive done. The next day I very nervously drove it 100 miles to Sywell Aerodrome for the VBOA rally, the manifold wrap was smoking for a good 70 miles of that, made me very nervous. But she made it!!!
I am a VERY VERY lucky boy and all I can say to everyone on the club is, GET A FIRE EXTINGUISHER IN YOUR CAR! having one on me, although it didn't keep the fire out, it did enough to hold back the flames until help arrived and saved my car. Best 20 quid I ever spent in halfords.
The rail will be refitted with a washer between the mount and rail which will space it enough that it clamps the injectors but with no tension!
strip down
Tried a few different things, panel wipe, brake cleaner, sponge etc. I then got the acetone out and this stuff was magic!! Tried it on the boost pipe and strut brace...
Mint!
Quick look at the bay
You can see
loom charred at the back and engine loom
hoses discoloured
powdercoat tarnish
paint black
header tanks black
powder hiding around
So I set to work with the Acetone and quick detailer after and this was the result
Pretty god damn good in my opinion!!! I am a very lucky and happy boy! The only things that wouldn't clean up are the header tank and brake fluid res.
Also, seems like the slam panel and bonnet in the same area were super heated and it melted the paint!
Deffo not the worst thing in the world, I can repaint the scuttle in winter and I actually wanted to repaint the bonnet anyway because there is a dent in it. Do that in winter too
So the rebuild began, fuel rail cleaned up, Injector were flow tested, no issues, new o rings fitted. This time, the saftey clips for the injectors were lockwired to the rail to stop them coming out if the rail every came loose again!
I forgot to take a photo, but the fuel rail is now drill n tapped from M5 to M6, it is now nut and bolted and the bolts are lock wired together! This rail is never coming loose again
Inlet cleaned and refitted. Acetone is a miracle worker!
New air filter and the whole car is back together the night before VBOA rally!
I warmed it up, gave it a foot full to the roundabout and back. Test drive done. The next day I very nervously drove it 100 miles to Sywell Aerodrome for the VBOA rally, the manifold wrap was smoking for a good 70 miles of that, made me very nervous. But she made it!!!
I am a VERY VERY lucky boy and all I can say to everyone on the club is, GET A FIRE EXTINGUISHER IN YOUR CAR! having one on me, although it didn't keep the fire out, it did enough to hold back the flames until help arrived and saved my car. Best 20 quid I ever spent in halfords.